Sunday, August 25, 2019

Microcosm II


      This time it began a couple of weeks ago.  I needed to fill ruts inside the combine shed with gravel.  I had a few other places that could use some gravel.  The GMC truck was sitting empty.  The G (John Deere tractor) hadn’t been moved for over a year.  I needed to mow where it sat in its aura of grass.
     I set out to knock over the first domino in a long line of dominoes that would eventually lead to me hauling some gravel from the pasture creek.  Step one, get the tractor started.  The battery came off the now-shedded combine and into the G. 
      It started right up.  Well, maybe my luck had changed.  It had a low rear tire, so I pulled it over and parked in front of the shop close to the air compressor.  I shut it off.    I dragged the air hose out and crawled under the tractor to access the tire valve.  I half expected to have to dodge some calcium chloride, but the inner tube was dry.
       (Calcium chloride is a water-based mixture used for ballast in tractor tires.  It probably weighs more than water and it stays low to the ground, gravitating to the bottom of the tire and inner tube, reducing chances of tractor rollover.  The solution is somewhat caustic to skin and especially eyes.  It is corrosive to metal.)
      A few minutes of air brought the left side of the tractor up to match the right side.  I crawled out from under the tractor.  Then I saw it.  A rip in the tire where the inner tube was starting to bulge through.
      That string of dominoes was going nowhere.  The rip was in the tread portion of the tire.  It wouldn’t take much at all to puncture that tube and I would be dead in the water.  Or more appropriately in the middle of the pasture or somewhere between pasture and farmyard.
      A new string of dominoes had to be erected.  I would have to get the farmhand off the tractor in order to get to the tire that has to be replaced. 
       There is a place in the south yard where I usually park the farmhand when I remove it.  Heavy cement blocks serve to hold up the farmhand when it is not on the tractor.  The site too was well endowed with tall grass. 
     I had to abandon the project for the time being.  I needed to get the ruts filled so I could park trucks in the shed.  One truck had seed wheat on it.
      I cleared off the bed of the 4X4, threw on a shovel and headed for the ditch just west of the mailbox where heavy rains deposit gravel when the water runs out of the field and across the road.  A couple of hours later, I had the ruts filled with some first rate gravel.  It was a hot day and I was tired after twice shoveling the gravel, onto the 4X4, and off the 4X4 into the ruts.  The G would have to wait.
      We move now to a couple of weeks later.  The G still sat in front of the shop.  I needed to get a few other things close to the shop.  The G would be out of service until further notice.  But I did need to move it.  And I should get that farmhand off of it.          
     Back to that string of dominoes.  In the intervening two weeks since I started the ill-fated project, the left side of the tractor slowly sank.  The tire was flat.  Oh well, air compressor is close at hand.
       I moved the heavy cement blocks that support the farmhand.  I took the Ford tractor and mower to the site and soon it looked all nice and neat.  With the golf cart, I hauled toolbox, bar, and jack, all things I would need to get the fork off the front of the farmhand and the farmhand off the tractor.
      Once again I drug air hose underneath the tractor and fastened the handy-dandy air chuck to the tractor tire.  After a minute or two, the tractor rose to near-normal level.  Then it was I heard an ominous hissing.  I crawled out from under the tractor.  The sound was easily located.  Through the afore-mentioned rip in the tire, I could see a pin holed, well, more like a nail hole in the inner tube.
      By widening the rip a little, I thought I could get a tire patch onto the tube, enough to hold while I got the farmhand off and the tractor parked where I could get to it to change the tire, if ever I could find a tire for it.  I would need to let the air out of the tire to get the patch to stick.
     Back under the tractor, I placed a jack to hold the tractor up while I repaired the tube.  I pulled the valve core out of the tube and let the air escape.  A little jerk with pliers opened the tire rip up enough to get glue onto the nail hole and then, after the glued dried appropriately, the patch.
     All went well.  But now the rip was even bigger and the tube might not take more than a revolution or two before it was punctured again.  I devised a boot, something like the mesh used to correct a hernia, used to plug a fissure in a tire.  I used an old inner tube folded over about five or six inches square.
     It wasn’t exactly laparoscopy, but it was similar.  With pliers and screwdriver, I force the folded inner tube through the rip into the tire between the tire and the tube.  For good measure, I cut a smaller chunk out of a plastic antifreeze jug and forced it in there, too.
     The slick plastic piece didn’t want to stay in place, so I finished off with . . . you guessed it, duct tape to stabilize the plastic patch.  Back under the tractor, I replace the valve core and once again hooked the air hose to the tire. 
      All was well.  No hissing.  I cleared away tools and jack and mounted the tractor.  It would not start.  I pulled spark plugs and cleaned them.  Fouled plugs are the usual reason the old thing won’t fire.  Plugs replace, I tried again.  Nothing!
     It was growing late.  I was tired.  Sometimes, if I let it set for a while, it will forget its abstinence and start right up.  Tomorrow.
      Tomorrow got here.  A look out the window showed the left side of the tractor much lower than the right side.  Oh well.  Maybe the tire would hold air long enough for me to complete my project.   After two hours of removing, cleaning, installing spark plugs, I had to give it up again.  The thing just would not start.
     A batch of expletives and hand gestures hurled at the G left it unmoved.  I pulled the spark plugs and left them out to give the cylinders a chance to dry out while I took a lunch break.  In my mind, I was writing the want ad:  “For sale, John Deere G with bad rear tire.  John Deere collector’s must-have.  With or without Farmhand.”
     I made one more try after the nooning.  I was interrupted by Jerrod and his son.  They came out to finish up some details of last January’s siding job.  Two lightning rod cables need to be fastened to the corners.  The big project was the roof flashings over back porch and west addition to the house. 
     They had installed them over the siding.  They should be behind the siding so that water running down the wall had nowhere to go but onto and off of the roof, no chance to get into the joint between roof and wall.  That took a couple of hours. It's all better now.  It looks much nicer with the flashing installed properly.
     After they left and I cleaned up, it was too late to try the G again.  If it started, it would be dark before I could get everything done.
      I gave it one more try the next day.  I got nothing, not one pop, no smoke, nothing.  Somewhere out of the fog of ancient memory, I remembered that when this happened in the past, new spark plugs made a difference. 
     It has a new magneto.  The spark plug wires check out ok.  It was getting fuel.  New plugs will be the next domino to try.  The new plugs won't say "Champion" on them if I can help it.
     Meanwhile, the G sits in front of the shop blocking the way for other equipment needing attention.  Blocks hold the left rear up so the weight of the tractor won’t cause other problems with the ancient tube and tire.
     And so it goes.   
         

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